TY - JOUR
T1 - UASB/Flash aeration enable complete treatment of municipal wastewater for reuse
AU - Khan, Abid Ali
AU - Gaur, Rubia Zahid
AU - Lew, Beni
AU - Diamantis, Vasileios
AU - Mehrotra, Indu
AU - Kazmi, A. A.
PY - 2012/8
Y1 - 2012/8
N2 - A simple, efficient and cost-effective method for municipal wastewater treatment is examined in this paper. The municipal wastewater is treated using an upflow anaerobic sludge bed (UASB) reactor followed by flash aeration (FA) as the post-treatment, without implementing aerobic biological processes. The UASB reactor was operated without recycle, at hydraulic retention time (HRT) of 8 h and achieved consistent removal of BOD, COD and TSS of 60-70% for more than 12 months. The effect of FA on UASB effluent post-treatment was studied at different HRT (15, 30 and 60 min) and dissolved oxygen (DO) concentrations (low DO = 1-2 mg/L and high DO = 5-6 mg/L). The optimum conditions for BOD, COD and sulfide removal were 30-60 min HRT and high DO concentration inside the FA tank. The final effluent after clarification was characterized by BOD and COD values of 28-35 and 50-58 mg/L, respectively. Sulfides were removed by more than 80%, but the fecal coliform only by ̃ 2 log. The UASB followed by FA is a simple and efficient process for municipal wastewater treatment, except for fecal coliform, enabling water and nutrients recycling to agriculture.
AB - A simple, efficient and cost-effective method for municipal wastewater treatment is examined in this paper. The municipal wastewater is treated using an upflow anaerobic sludge bed (UASB) reactor followed by flash aeration (FA) as the post-treatment, without implementing aerobic biological processes. The UASB reactor was operated without recycle, at hydraulic retention time (HRT) of 8 h and achieved consistent removal of BOD, COD and TSS of 60-70% for more than 12 months. The effect of FA on UASB effluent post-treatment was studied at different HRT (15, 30 and 60 min) and dissolved oxygen (DO) concentrations (low DO = 1-2 mg/L and high DO = 5-6 mg/L). The optimum conditions for BOD, COD and sulfide removal were 30-60 min HRT and high DO concentration inside the FA tank. The final effluent after clarification was characterized by BOD and COD values of 28-35 and 50-58 mg/L, respectively. Sulfides were removed by more than 80%, but the fecal coliform only by ̃ 2 log. The UASB followed by FA is a simple and efficient process for municipal wastewater treatment, except for fecal coliform, enabling water and nutrients recycling to agriculture.
KW - Diffused aeration
KW - Fecal coliform
KW - Municipal wastewater
KW - Nutrients recovery
KW - Sustainable treatment
KW - UASB post treatment
UR - http://www.scopus.com/inward/record.url?scp=84865341717&partnerID=8YFLogxK
U2 - 10.1007/s00449-011-0675-z
DO - 10.1007/s00449-011-0675-z
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C2 - 22218993
AN - SCOPUS:84865341717
SN - 1615-7591
VL - 35
SP - 907
EP - 913
JO - Bioprocess and Biosystems Engineering
JF - Bioprocess and Biosystems Engineering
IS - 6
ER -